Tkerrigan22
Member
Hey Everyone,
I need some help on this. I just maidened my new rotor bones spider quad and everything went well. The next day I flew again and the quad pitched forward several times and gained so much forward momentum that it slammed into my shed. I am flying with a KK2.1.5 control board with the following settings:
Control Board: KK2.1.5
PI Values:
Roll Axis (Aileron)
Pgain: 41
Plimit: 100
Igain: 25
Ilimit: 20
Pitch Axis (Elevator)
Pgain: 41
Plimit: 100
Igain: 25
Ilimit: 20
Yaw Axis (Rudder)
Pgain: 40
Plimit: 20
Igain: 50
Ilimit: 10
Self Level Settings
Pgain: 50
Plimit: 20
Acc Trim Roll: 0
Acc Trim Pitch: 0
https://www.youtube.com/watch?v=2qkBYu0A5rI
I have attached the video that I captured so that you can see how it was behaving. Does anyone have experience with this, or any ideas of what could have happened? The KK2 board was calibrated prior to my first flight.
I need some help on this. I just maidened my new rotor bones spider quad and everything went well. The next day I flew again and the quad pitched forward several times and gained so much forward momentum that it slammed into my shed. I am flying with a KK2.1.5 control board with the following settings:
Control Board: KK2.1.5
PI Values:
Roll Axis (Aileron)
Pgain: 41
Plimit: 100
Igain: 25
Ilimit: 20
Pitch Axis (Elevator)
Pgain: 41
Plimit: 100
Igain: 25
Ilimit: 20
Yaw Axis (Rudder)
Pgain: 40
Plimit: 20
Igain: 50
Ilimit: 10
Self Level Settings
Pgain: 50
Plimit: 20
Acc Trim Roll: 0
Acc Trim Pitch: 0
https://www.youtube.com/watch?v=2qkBYu0A5rI
I have attached the video that I captured so that you can see how it was behaving. Does anyone have experience with this, or any ideas of what could have happened? The KK2 board was calibrated prior to my first flight.