Binding DONE. But no output ppm from FS-i6AB RX

percyjackson007

New member
I have tested the ppm output of my receiver, with an arduino pulseIn function, and also tried a servo motor to test it. Both the times, there is no output in any of channels, except channel 1, which has a randomized noise. The values range from 800-1300 on channel 1 which fluctuates constantly, like a vibration. When I connected my servo on CH1, it was legit vibrating.

One of my senior with experience said, either the RX isn't receiving enough current. (Even though it did bind, and I could read a full battery level in my TX). Or the RX is messed up.

He suggested to either get it repaired or get a new one.



Is there anyone with a similar experience or answer to this issue?
 
Last edited by a moderator:

PsyBorg

Wake up! Time to fly!
@percyjackson007 @Bifi.baarlo Guys change the language mates. Adding stars to bad words is STILL using bad words. Lets not back slide slowly into general internet levels. Lets make an effort to keep things right here. Besides if a mod or dev sees it you'll get smacked with a warning or ban anyways.