percyjackson007
New member
I have tested the ppm output of my receiver, with an arduino pulseIn function, and also tried a servo motor to test it. Both the times, there is no output in any of channels, except channel 1, which has a randomized noise. The values range from 800-1300 on channel 1 which fluctuates constantly, like a vibration. When I connected my servo on CH1, it was legit vibrating.
One of my senior with experience said, either the RX isn't receiving enough current. (Even though it did bind, and I could read a full battery level in my TX). Or the RX is messed up.
He suggested to either get it repaired or get a new one.
Is there anyone with a similar experience or answer to this issue?
One of my senior with experience said, either the RX isn't receiving enough current. (Even though it did bind, and I could read a full battery level in my TX). Or the RX is messed up.
He suggested to either get it repaired or get a new one.
Is there anyone with a similar experience or answer to this issue?
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