I plugged it all together to mark the max servo positions for the flaperon push rods - sadly the rudder servo wire smoked - with that servo cable removed, luckily everything else is working - I am perplexed as to why the servo shorted on the wire and hopefully it can be repaired as the A10 is a great servo.
Here is a quick test with the flaperons hooked up - there is plenty of throw but the end points are dialled back at the moment as the program is from my BAMFzilla and will need to be tuned for the Phantom 2.